Update #1
I repaired the insulation on the wire that was chaffed using liquid electrical tape. I modified the plug a little that goes into the ECU so the pressure points were relieved and wrapped the wires with the spiral wire loom for some extra protection.
Update #2
I thought one spark plug was loose. ALL 8 spark plugs were loose. I can't be absolutely, positively, 100% sure that the shop did not tighten the plugs down correctly. I don't remember pulling the plugs when I winterized and I am 99.99999% sure I did not, but without being sure it's hard to place blame. So, all the brand new plugs came out and 8 brand new ones went in. This time AC-Delco 41-983 gapped to .060 and torqued to 22 ftlbs with a stop at 11 ftlbs.
I have a feeling my problems are going to be gone the next time I fire the boat up.
_________________________
James
2002 Cobalt 226 VP 8.1GIDP
2007 Chevy 2500HD Crew Cab Duramax
1988 Suburban 3/4 Ton
2005 Subaru Forester XT (Turbo)- FOR SALE
2000 Subaru Forester
1965 Mustang